KeithB
Resident Half Fast Machinist
I've had an Enco brand 10' x 54" vertical milling machine since 2000. It has given good service - the ways, table and screws are all in good shape, but the head had suffered some mechanical problems. The powered downfeed gave out, then the low speed gear range broke. Finding parts for a slightly off-spec Taiwanese mill was impractical. Fortunately there are complete replacement heads available so I decided to simply replace the whole head. I wanted a functional mill, not a long term repair project.
Enco 10" x 54" vertical mill with broken step pulley type head. The box end wrench on the front is on one of the clamp bolts, the ratchet on the rear drives a worm to tilt the head left and right.


I settled on a variable speed mechanical head sold by H H Roberts Machinery Limited in Ontario Canada. Very good folks to deal with! They also sell electronic drive heads that can be interfaced with CNC controls but I have a CNC mill and really just need a good mechanical mill thus my choice.
Replacement head from HH Roberts Machinery Limited.


The first step was to remove the old head. After shutting the breaker off at the box I disconnected the four wires at the machine. Then I loosened up the four bolts on the face of the machine head and used the worm screw drive on the head to rotate the head from the vertical to the horizontal orientation. I made a cradle out of some wood and raised the knee up to support the head on the table. With the weight securely supported by the table I took the nuts all the way off and used the Y axis screw to pull the head forward and off the bolts. Then the hydraulic foot lift was used to move the head to a steel table. I did all this myself over a weekend, a lot of it from a wheelchair. Not all that hard if you think things through and use the right tools!
When Scott came in we attempted to put the old head on by doing the reverse - lift the new head up on the cradle with the footlift, sit the cradle on the table and use the knee elevation and the Y axis screw to slide the head over the four bolts, tighten the bolts up until slightly snug and crank the head up to the vertical position. The hardest part was getting four loose bolts sliding around in a circular T-slot to line up with the holes in the head. They even make the holes in the machine head larger than the bolts and then provide bushings to slide over the screws and into the machine head after the bolts are through! It was like herding cats!
We finally got the head on over the bolts (and were exhausted by the effort) when we ran into a problem. The head jammed up when we got it about a half inch away from meeting up with the face of the ram trunnion. My friend Mike - he's a machinery rigger - brought by an electric floor crane and let us use it. It made handling the head a lot easier. We pulled the head back off the bolts and looked at it very carefully. There were indentations on the edges of the opening of the new head that were made by the gear teeth of the gear in the trunnion face. The gear was larger than it should be and wouldn't mate up.
Trying to put head on using footlift. Note spur gear bolted to center of trunnion.

My friend Mike with the CatCart elecric floor crane.

To be continued...
Enco 10" x 54" vertical mill with broken step pulley type head. The box end wrench on the front is on one of the clamp bolts, the ratchet on the rear drives a worm to tilt the head left and right.


I settled on a variable speed mechanical head sold by H H Roberts Machinery Limited in Ontario Canada. Very good folks to deal with! They also sell electronic drive heads that can be interfaced with CNC controls but I have a CNC mill and really just need a good mechanical mill thus my choice.
Replacement head from HH Roberts Machinery Limited.


The first step was to remove the old head. After shutting the breaker off at the box I disconnected the four wires at the machine. Then I loosened up the four bolts on the face of the machine head and used the worm screw drive on the head to rotate the head from the vertical to the horizontal orientation. I made a cradle out of some wood and raised the knee up to support the head on the table. With the weight securely supported by the table I took the nuts all the way off and used the Y axis screw to pull the head forward and off the bolts. Then the hydraulic foot lift was used to move the head to a steel table. I did all this myself over a weekend, a lot of it from a wheelchair. Not all that hard if you think things through and use the right tools!
When Scott came in we attempted to put the old head on by doing the reverse - lift the new head up on the cradle with the footlift, sit the cradle on the table and use the knee elevation and the Y axis screw to slide the head over the four bolts, tighten the bolts up until slightly snug and crank the head up to the vertical position. The hardest part was getting four loose bolts sliding around in a circular T-slot to line up with the holes in the head. They even make the holes in the machine head larger than the bolts and then provide bushings to slide over the screws and into the machine head after the bolts are through! It was like herding cats!
We finally got the head on over the bolts (and were exhausted by the effort) when we ran into a problem. The head jammed up when we got it about a half inch away from meeting up with the face of the ram trunnion. My friend Mike - he's a machinery rigger - brought by an electric floor crane and let us use it. It made handling the head a lot easier. We pulled the head back off the bolts and looked at it very carefully. There were indentations on the edges of the opening of the new head that were made by the gear teeth of the gear in the trunnion face. The gear was larger than it should be and wouldn't mate up.
Trying to put head on using footlift. Note spur gear bolted to center of trunnion.

My friend Mike with the CatCart elecric floor crane.

To be continued...










